Difference between revisions of "2015.07.26.Crash"

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Revision as of 15:03, 4 September 2020

2015.07.26.AccidentFig2.4.1-2.png Tail part of the ailplane crashed [1]

ChofuOshimaMa.png Chofu and Oshima

2015.07.26.CrashTrajectory5.png Trajectory estimated


2015.07.26.Crash referes to catastrophe of small airplane Piper PA-46-350P, registered JA4060, near the Chofu airport, soon after take-off.

Few strange details from the original reports [2][1] about that crash are mentioned below.

Overview

The report [1] suggests the following summary:

On Sunday, July 26, 2015, at around 10:58 Japan Standard Time (JST: UTC + 9hrs:unless otherwise stated, all times are indicated in JST using the 24-hour clock), a privately owned Piper PA-46-350P, registered JA4060, crashed into a private houseat Fujimi Town in Chofu City, right after its takeoff from Runway 17 of Chofu Airport. There were five people on board, consisting of a captain and four passengers.
The captain and one passenger died and three passengers were seriously injured. In addition, one resident died and two residents had minor injuries.The aircraft was destroyed and a fire broke out. The house where the aircraft had crashed into were consumed in a fire and neighboring houses sustained damage due to the fire and other factors.

Destination was Oshima Airport.

Speed and altitude

2015.07.26.CrashT.png 2015.07.26.CrashD.png

Figures as left show reconstruction of trajectory of the aircraft before the crash, images are from the same report [1].

The red curves shows altitude of the aircraft versus time (JST) and versus distance from the runway threshold. Following the old tradition (established before discovery of the rotational symmetry of the space), the length is measured in meters, while altitude is measured in foots.

Figures show, that at 40:57:45, the aircraft passes the threshold at altitude 25 ft with seed 87 knots.

Figure 1.16.5.4, at page 60 of the same report, indicates that, approxmately at this moment, namely, at 10:57:50, the landing gear is retrtacted. Perhaps, the retracting of the landing gear takes of order of 5 second; so, the deviation of 5 seconds is not significant.

Then, the aircraft seems to loss the control; the pitch and speed become chaotic. The shaking leads to loss of speed, and the aircraft falls down to the living blocks. In the report, the coincidence of the retracting gear and loss of the control is not discussed.

In the next section, this coincidence is discussed; the lost of control is interpreted as result of some defect or mechanism that is switched on at the retraction of the landing gear.

Conspirology

2015.07.26.CrashAnnunsiator0.png 2015.07.26.CrashLandingGearWarning.png


2015.07.26.CrashMap.png   page 60, Figure 2.16.5.4 Estimated Flight Route

The problem of the aircraft appears at the retracting of the landing gear.

The figures indicate, that, after an attempt to retract the landing gear, the aircraft losses its performance; both speed and pitch become incontrolable. In addition, the averaged speed, instead of to increase (due to reduction of the aerodynamic drag of the wheel), reduces.

Figure 2.16.5.7(3) at page 63 confirm, that the landing gear was not successfully retracted at least until 10:57:53. (After the retraction of the landing gear, the lighting of the gear indication is supposed to be off.)

At this moment, the aircraft gets out of control, losing both speed and altitude.

The coincidence above could be interpreted with hypothesis, that some object happened in the place, where the wheels of the aircraft are supposed to be packed. The squeezing had affected the cables from the cabin to the tail, and leaded to the lost of control.

Perhaps, the Captain tried to regain the control, accelerating the aircraft in various directions, but the reserve of speed and altitude was not sufficient. Perhaps, there was no sufficient time to release the landing gear back, in order to regain the control of the aircraft. That would allow to perform the emergency landing at the same airstrip, or even to continue flight with landing gear released, until the amount of fuel reduce, and speed and altitude increase sufficiently for the safe retraction of the landing gear.

Perhaps, at the heavy load and displacement of center of mass behind the optimum, the aircraft (and lives) still can be saved, delaying the retraction of the landing gear for a minute, until the aircraft gets sufficient speed and altitude.

Perhaps, at the uncontrollable "nose-up", the aircraft and lives can be saved, if the Captain ask passenger to move forward, at least for one or two meters.

The last hypothesis could be checked (verified of refuted) by the sportive pilots, performing the manoevres with heavy load, "center mass behind the optimum", with releasing and retracting of the landing gears and "noise-up" at the altitude, sufficient for the recovery to the safe flight conditions.

The hypothesis above differs from the interpretation in figure 3.5.3 of the Report. According to that figure, the aircraft took-off a hundred meters before the optimal position (and before it got the speed sufficient for the safe launch), and this is interpreted as one of the main causes of the accident.

The hypothesis in this section is provoked by some questions that arise at the reading of the English version of the Report. These questions are mentioned below in the special section.

Questions

The English version of Report [1] causes questions. The primitive (and, perhaps, not appropriate) attempt to clarify them is presented above in section "Conspirology". However, suth a "conspirology" helps to formulate the questions in sharp form below:

1. According to the Report, for a flight for a distance of order of 100km, the fuel had been loaded in amount, sufficient for a flight to a distance more than 1000 km.
Is it normal practice, to load fuel in amount of an order of magnitude larger, than necessary for the flight?
Is such a practice usual in the world-wide small aviation?
In Japan?
At the Chofu Airport?

2. Fluctuations of speed with frequency of order of 1 Hz are seen in figure 2.16.5.3-3.
Amplitude of these fluctuations is of order of 4 ft/sec.
This corresponds to acceleration
\( 2 \pi \times 1 \mathrm{Hz} \times 4 \times 30.48 \mathrm{cm}/\mathrm{s} \approx 7.7 \mathrm{m/s^2} \approx 0.8 g \),
were \( g\approx 9.8 \mathrm{m/s^2} \) is the free-fall acceleration.
Such an acceleration is supposed to cause strong discomfort of the passengers.
(It is of order of acceleration at the emergency braking of a car.)
Neither records, nor the aposteriori statements of the survivors confirm, that they felt this discomfort during last 10 seconds of the flight.
Why the Report does not mention this disagreement?

3. The cause of the strong fluctuations of the speed is not revealed.
Is the rotation speed and inertion of the propeller sufficient to allow short acceleration and decceleration with amplitude of order of \(g\)?
Could the strong fluctuations of speed and pitch be result of attempts of the Captain to regain the control, to push out some garbage, that could block the cables to the elevators at the retraction of the landing gear?

4. According to the Report, the stall speed for the aircraft is of order of 70 knots.
However, it depends also on the mass and on the acceleration of the aircraft.
According to the graphics suggested, at the moment of retracting of the landing gear (10:57:45 - 10:57:53), the speed was not below the stall.
As the necessary vertical speed was already achieved, the vertical acceleration was supposed to reduce, but it seems to increase at the moment of retracting of the landing gear. Can the loss of stability be somehow related with the retracting of the landing gear?

5. Before retracting the landing gear, the power of motor is sufficient for stable flight with increase of both, speed and altitude.
After the retracting the landing gear, the power becomes not sufficient; the control seems to be lost in both pitch and roll.
Could the control on the airplane be recovered with emergency extension of the landing gear?
Can the uncontrollable "nose-up" be mitigated, softened and/or ever resolved with the emergency extension of the landing gear?
Can this solution be recommended for pilots, who suddenly happen in a similar situation?

6. Do the questions above address only to the English version, or they can be applied to the Japanese original too?

References

  1. 1.0 1.1 1.2 1.3 1.4 2017.07.18. https://www.mlit.go.jp/jtsb/eng-air_report/JA4060.pdf AA2017-4AIRCRAFT ACCIDENTINVESTIGATION REPORTPRIVATELY OWNEDJ A 4 0 6 0 July 18, 2017 The objective of the investigation conducted by the Japan Transport Safety Board in accordance with the Act for Establishment of the Japan Transport Safety Board and with Annex 13 to the Convention on International Civil Aviation is to determine the causes of an accident and damage incidental to such an accident,thereby preventing future accidents and reducing damage. It is not the purpose of the investigation to apportion blame or liability.Kazuhiro NakahashiChairmanJapan Transport Safety BoardNote:This report is a translation of the Japanese original investigation report. The text in Japanese shall prevail in the interpretation of the report.// CRASH AFTER TAKEOFFPRIVATELYOWNEDPIPER PA-46-350P, JA4060CHOFU CITY, TOKYO METROPOLITAN, JAPANAT AROUND10:58 JST, JULY 26, 2015July 7, 2017 Adopted by the Japan Transport Safety Board Chairman Kazuhiro Nakahashi// Member Toru Miyashita// Member Toshiyuki Ishikawa// Member Yuichi Marui // Member Keiji Tanaka // Member Miwa Nakanishi ..
  2. 2017.07.18. https://www.mlit.go.jp/jtsb/aircraft/rep-acci/AA2017-4-1-JA4060.pdf AA2017-4航 空事 故 調 査 報 告書 I 個人所属 パイパー式PA-46-350P型 JA4060 墜落 AA2017-4航 空事 故 調 査 報 告書I 個人所属 パイパー式PA-46-350P型 JA4060 墜落 平成29年7月18日運 輸 安 全 委 員 会Japan Transport Safety Board // 本報告書の調査は、本件航空事故に関し、運輸安全委員会設置法及び国際民間航空条約第13附属書に従い、運輸安全委員会により、航空事故及び事故に伴い発生した被害の原因を究明し、事故の防止及び被害の軽減に寄与することを目的として行われたものであり、事故の責任を問うために行われたものではない。 運 輸 安 全 委 員 会 委 員 長 中 橋 和 博

https://en.wikipedia.org/wiki/Piper_PA-46

https://cutteraviation.com/cutter-piper-sales/aircraft/piper-mirage-pa-46-350p/ ..

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As you equip and price your Piper Mirage using the specifications below, do so with the knowledge that every dollar you spend takes you to a higher level of speed, comfort and capability.
SPECIFICATIONS - Piper Mirage Piper PA-46-350P
Max Cruising Speed: 213 ktas (395 km/h)
Range with 45 Minute Reserve 1,343 nm (2,491 km)
Standard Useful Load 1,212 lbs (549 kg)
Number of Seats Six (6)
Maximum Approved Altitude 25,000 ft (7,620 m)
Engine Lycoming Dual Turbocharged TIO-540-AE2A, 350 hp
Wing Span 43 ft (13.1 m)
Length 28.9 ft (8.8 m)
Height 11.3 ft (3.4 m)
Cabin Length 148 in (375.9 cm)

Keywords

2015.07.26.Crash, Crash, English, Japan